August 29th, 2009 Posted in News | Comments Off
Today the department reached a milestone in the restoration of Union Pacific 428. A fire was lit and the boiler was steam tested to approximately 200 PSI. This was the first fire in the locomotive since it was taken out of service by the UP in 1958.

Coal smoke fills the air as Union Pacific 428 comes alive for the first time in over 50 years.
The locomotive was filled using water from the bottle car and was pre-heated to about 100 degrees with the pool heater by Bill and the crew. The safety valves were installed by Jason and Matt and had been calibrated by a licensed shop prior to installation. Valves were checked, double check, and triple checked to ensure that they were in the proper position for the test.
The locomotive was then moved outside the shop by Ralph, Jason, Jeff, Mark and Ed to install the stack fan and light off the fire. Collin, Rick, and Greg used the boom truck to lift the heavy stack fan in place after the truck’s battery was jumped off Jim’s car because it was dead. A fire was built using coal, wood, and paper and was lit off at 2:06 PM and was slowly built up to start heating the water. The needle of the steam gauge moved off the peg about 40 minutes later, and the pressure was slowly brought up to check for leaks.

Ralph throws the first lumps of coal into the firebox to build the test fire.

The fire is started!
At about 50 lbs of pressure, the blower was opened and worked flawlessly. At about 60lbs, the fireman’s side injector was tried, and worked flawlessly at first as well. The engineers injector had some issues picking up water, and it we decided to scale back the fire until both injectors were operating.
Pressure slowly climbed. We discovered that the Fireman’s side check valve was not seating and once this problem was addressed, we continued to slowly raise the pressure of the boiler until the safety valves popped. The sight glasses were checked and cycled and the locomotive was blown down multiple times throughout the test. There were some other leaks found such as 3 flexible stay bolt caps, the engineer side water glass fittings, and some other tiny issues. All in all, it was a successful first test and we have more work to do in order to fix these problems and try again.
One of the highlights of the afternoon was the blowing of the whistle. Its tone leaves something to be desired, but it was nice to hear the “voice” of a locomotive that had been silenced over 50 years ago.

The steam gauge.

Jason watches as the safety valve lifts for the first time.
Ralph and Jason oversaw the test with help from Jim, Nigel, Tom, Vince, and Matt.

Ralph blows the whistle as Jason reaches for the injector to put some water into the boiler
Thanks to the B&G department for helping with the test by providing a Bobcat tractor to act as a coal bunker and for loading of the coal onto the deck of the locomotive.
Not to be overlooked was the work done by Bruce, Stu, Tammy, and Jim on 1630 bearing boxes. The wear plate for the second box was filed and fitted in place on the box so final installation can begin next week. The other driving box is nearing completion but needs final machining to cut down the excess crown brass stock and to cut grease grooves This project along with work on the Shay was going on simultaneously with the steam test
The success of this initial test was moderate, at best, but was a large accomplishment for the department. After more than 25 years of work, it was proven that the locomotive’s boiler is sound and is capable of producing steam. In the coming weeks the problems we found will be addressed and another test may occur before the end of the season if weather permits. Feel free to stop by the shop and check out the progress of this project as well as the other going on in the shop as well.
Matt
All photos by Matthew Dowd